Allocative efficiency, potential cost savings, and power supply price markdown in Korean electric power sector
Myunghun Lee
Energy & Environment, 2019, vol. 30, issue 4, 617-628
Abstract:
As one publicly owned company monopolizes the electricity supply, Korea’s power market has been distorted. Firms faced with constraints imposed by a regulatory environment are likely to fail to minimize their production costs subject to market prices. In this paper, we test for allocative efficiency of fuel inputs for the Korean electric power industry over the period of 1990–2015. The potential cost savings and maximum power supply price markdown are calculated by imposing allocative efficiency. The power plants, on average, could have reduced their fuel costs by as much as 22.1% annually. The attainment of allocative efficiency would have enabled the power supply price to be cut by 7.6% annually.
Keywords: Allocative efficiency; shadow cost; cost savings; supply relation; power price markdown; electric power sector (search for similar items in EconPapers)
Date: 2019
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Persistent link: https://EconPapers.repec.org/RePEc:sae:engenv:v:30:y:2019:i:4:p:617-628
DOI: 10.1177/0958305X18802767
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